PowerLabs Rail Gun Research Progress! |
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This page carries the images and
videos of the Rail Gun construction effort; a 120-hour endeavor that cost
approximately $800 of my own money, not counting sponsor-supplied materials. All images are high resolution; the original can be seen by
clicking on the thumbnail. This page is no longer being updated. For current information on project status and testing progress please go to the Rail Gun Testing Page. |
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Day-By-Day Project advances and current project status: |
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10/18/02: The gun is READY for the presentation tomorrow (120 hours of work). Today I put the stickers on and checked everything electrically. It has not been tested because I do not have a H.V. charging power supply, but I have enough faith in my design and I have tested everything aside from an energized rail test to be fairly confident that it should work. Tomorrow it will be fired for the first time ever at the Wisconsin Dells Teslathon. I had 4 people scrutinize my design today; The master machinist at the ME department, two machine shop supervisors at the shop where I work, and my project advisor. This is what I will need before I can fire the gun at the University laboratories:
1-
Plastic Projectile Ram Rod. 10/17/02: Two days to go. Added current limiting charging resistor (225W 900Ohms) and safety discharge resistors (4x 25000Ohms 75W in parallel), also made some High Voltage and Stored Energy warning stickers for the gun (University Public Safety actually requires this), added a sticker from my sponsor for the capacitor bank.
10/16/02:
Today I got the ultra pure aluminum bar (1100Al) for my projectiles. First
I milled it down from 1/4" thickness to 0.23" (the rail spacing), and than
I milled it from 1" width to 0.630". I used the foot long machined bar to
re-set the spacing on the entire Rail Gun, so that the bore is now
perfectly straight and VERY tight fitting for the projectiles. I than cut
a couple of inch long projectiles, each one weighting approximately 6
grams (density for Al = 2.7g/cc). I fitted one into the barrel and fired
it with 100PSI using the machine shop air line. To my surprise it came out
fast enough to blast right through the welding booth protective screen! I
tried a second shot today with 300PSI at the lab. According to the program
Slava wrote me to simulate the injector's performance the exit velocity
should be just under 200m/s (700fps). I am not sure what the actual value
was but it cut right through the box I had to stop it and ended up hitting
a piece of wood behind the box. THIS IS AS POWERFUL AS THE INJECTOR CAN
BE. According to the program the injector should be imparting 120joules of
Kinetic energy into the projectile. I also finished wiring the gun and
making High Voltage connectors for it: Tomorrow I hope to get speed
measurements for the injector and MAYBE (unlikely) do some powered
testing.
10/15/02: After only a couple of shots with air in the Rail Gun the rails were literally spitting out the PFA film insulator and Vinyl tape I was using to keep them from contacting the projectile until it had 2 and a half inches of rails behind it (this is important because without a stable magnetic field behind it to push it forward the projectile will either jump back or not accelerate at all on meeting the rails). I devised what I now thing to be the best solution for the problem; I ordered a 12x12" 1/32" thick Glass Fibre filled PTFE (Teflon) sheet, machined the rails down to 1/31", cleaned everything with industrial degreaser, applied plenty of metal/plastic epoxy to the rails and glued the sheets under pressure. It is impossible to glue fluoropolymers (specially Teflon) unless they have been chemically treated. Melting them in place is also not an option. My hope was that because it is glass filled this sheet would adhered thanks to its porosity. I seem to have guessed right; the sheet seemed very rough and abrasive and bonded (as far as I can tell) nicely to the copper, but after I ran a sharpened mill bit over them they became perfectly smooth and slippery (glass filled PTFE has almost the same coefficient of friction as Teflon). This looks like a good solution. 10/14/02: First day in months that I don't machine something at the shop. Today I hooked up a dual trace 60MHz Oscilloscope to the Rail Gun, charged it up to 14.5V with a DC power supply and obtained waveforms for discharges with both the entire rail length (short circuited by a piece of copper at the end) and for the beginning of the rails switched by a projectile. The shortest pulse obtained was 63.4uS for the entire rail length. The projectile switched pulse was longer, owning to the fact that the low voltage used did not allow for a high current to flow through the relatively poor connection between the rails and projectile. Voltage reversal was 16%. Everything is looking up for the high power test on Wednesday! More information about the waveform analysis to be posted on the Rail Gun page. Click on the test setup to watch the projectile switched discharge test video.
10/12/02: Today, exactly one week away from the Wisconsing Dells Teslathon where I hope to present the Rail Gun, the device is COMPLETED and READY TO BE FIRED. The entire gun was disassembled and the rails were thoroughly cleaned with degreaser and pure Isopropyl alcohol. I than milled the first inch and a half of the contact face to be 0.001" lower than the rest of the rails and put Vinyl tape over that. I than experimented with Teflon tape as a means of insulating the other inch of the rails but that did not work (too fragile). I resorted to PFA film for the last inch; it is stronger than Teflon and has the same 500F working temperature. This is a very critical part of the gun; if the projectile scratches or melts this tape it will contact the rails too soon and acceleration will be non optimal. I am currently looking into better ways of ensuring that power is applied only after the projectile has some rail length behind it. Below you will see some pictures of the completed device. Although the gun is ready I still have some optimizations to make; namely installing bleeder resistors across each cap sub bank, installing charging/discharge resistors on the spark gap, and wiring the 24K gold plated HV connectors to the bank. Time to go out and party to celebrate this major stepping stone in my project :) Monday I will test it under power and obtain current waveforms of the discharge.
10/11/02: T-8 and counting. 8 hours of work today; Despite very close manufacturing tolerances it is normal for electrolytic capacitors to have very large variations in capacitance due to the chemical nature of their dielectric. In order to avoid unequal current distribution which can be very harmful to the capacitors at the extremely high current levels my gun will be running it is desirable to have all the capacitor values as close to each other as possible. My solution for that was to divide the 32 capacitors into 8 banks of 4 parallel capacitors each. By doing that instead of wiring them all individually I can make the current distribution more equal and also make the pulse waveform more uniform. Still, there was the problem of how to arrange them all so that each sub bank of 4 would have the same capacitance of the other 8 sub banks. My friend and fellow scientist Slava Persion from SVBx Labs came up with a very clever Genetic Algorithm program that finds the solution in less than a couple of seconds. If every combination were to be tried blindly it would take 5.5 * 10^22 years to find the solution (on a P4, 1.9GHz).. After a few seconds the program was able to arrange all 32 capacitors in such a fashion that each sub bank only varies 0.02% from the average of 6176.5uF. With the optimum configuration in hand I disassembled the entire capacitor bank, cleaned out the capacitor box and every single capacitor individually, drilled and installed the 24K gold plated high voltage connectors on the side of the box, and re-assembled the capacitor bank. I also disassembled the entire Rail Gun, but didn't get around to working on it because I had a party to go to :)
10/10/02: T-9 and counting. 4 hours of machine shop work today (had an exam at 6PM) and now the two power bus slots are cut on the capacitor box and all the wires are silver soldered in place at the capacitor end terminal busbars. Tomorrow I will re-arrange all the capacitors so that each sub bank of 4 caps has the same capacitance and also install the HV connectors for the gun. The project will than be done, minus the bleeder and discharge resistors that is. I am currently looking for a supplier for those.
10/09/02:T-10 and counting. 5 hours today: Finished off the spark gap today and milled one gap for the rail wires. The gun/cap bank combo is heavy enough that I am starting to struggle in getting it on and off the work table and carrying it around the shop so I went off and bought 4 small wheels and bolted them under the capacitor box. Went down to the machine shop, pressure tested the injector to 310PSI, and than fired the gun (just air) at 300PSI multiple times to evaluate what the recoil does with wheels on (it rolls back almost 1cm). Here is what it sounds like at 300PSI: Maximum Power Dry Firing Video. Tomorrow I want to solder the wires in place and thus finish the gun. Still have to buy resistors and install the connectors on it, but I will do those later on. I also have an oscilloscope on order for the lab so I should have circuit discharge waveforms shortly. Aside from machining a few projectiles my work at the machine shop for this gun is almost complete :) 10/08/02: T-11 and counting. 7 hours of machine shop work today; drilled, threaded and countersunk all the holes for the box top and the attachments for the gun to the capacitor box top. Also drilled/countersunk/threaded the holes for the spark gap attachment into the capacitor box. I spent ages with the master machinist at the shop making a moving electrode for the adjustable spark gap at the lathe and than the electrode broke off, so I'll have to do that again tomorrow. I filmed a close up video of the gun being fired with air at 100PSI so that I could observe the water condensation after the barrel. It is quite interesting. I also fired a nylon washer out of the gun into a can using the shop's 100PSI air line as a gas source. The washer was 1/8" thick and also smaller than the rails in width so it didn't come close to sealing the 1/4" x .6" barrel a huge gap in all directions inside the barrel, but it still came out fast enough that on hitting the bottom of the can it broke off in two pieces and sent the can flying backwards. Very neat video, definitely worth watching. Click on the pictures below to download the respective videos.
10/07/02: T-12 and counting. I was at the machine shop today from 5PM
to 8:30PM and finished most of the capacitor bank box. Now it has a 2"
wide triangle in each corner where the top will bolt to and a wide
polycarbonate bar across the middle to give it more structural rigidity.
Also cut, machined and drilled the two end terminals. Tomorrow I will
drill, thread and countersink 8 bolt holes through the top and box,
install the spark gap, and than try to make a mount for the gun to couple
to the box top. We'll see. After that all that I just have to solder the
wires into the capacitor terminals, make connections inside the bank,
install the resistors, and it will be DONE! 10/04/02: Glued the capacitor bank box together, something that involved 3 hours of careful manipulation of all sorts of clamps, weights and trigonometric instruments, as well as the inhalation of enough 1,2 Dichloroethane to pass out a horse. The capacitor bank was such a tight fit inside the box that if all the bolts didn't line up perfectly it simply would not fit! Talk about close tolerances :) I than went to a bodybuilding seminar by Cornelius Junior and came back to the machine shop for another 3 hours of machining, I cut, milled, glued, drilled and tapped 5 pieces of 1/2" polycarbonate and assembled the safety variable spark gap that will protect the bank from overcharging and also provide a means of manually discharging it from outside the box without having to come into contact with the live circuit. Needless to say, this spark gap will be current limited. A non current limited discharge from this bank would explode the gap to pieces.
10/03/02: Drilled and bolted down the 0.064" thick oxygen free copper bus bars that connect all 32 capacitors in the Rail Gun 20kJ 360MW power supply. Tomorrow I will cut, mill and drill the two end terminals and figure out a way of connecting them to the 16 oxygen free AWG 8 wires that go to the rails. I also hope to do some more work on the capacitor bank box. Maybe add wheels and a handle to it, considering how heavy this is turning out to be :-/
10/02/02: First test
firings: Machined and drilled the rest of
the capacitor busbars today. Looks like they will need some more work
before I can get everything to fit. Today I wired a push button switch to
the injector valve, connected the tank to a 2600PSI air tank with a
regulator and attempted a few discharges; first a 200PSI dry shot (very
loud, the gun sounds like a pistol) which blew some pieces of wood off the
ground a couple feet ahead of the muzzle. Secondly a 100PSI shot with a
very large and heavy copper projectile, and finally, a 200 PSI shot with
the same projectile, which consisted in a very poorly fitting copper bar
some .25x.55x3". The projectile was very heavy and didn't seal very well
with the barrel, so these shots by no means represent what the injector is
capable of, nor what the gun will ultimately be shooting.
10/01/02: The objective today was
to machine new projectiles for the injector and video a test firing at
high pressures. After hooking up the compressor to the injector tank I
found out that as feared the compressor was destroyed during previous
tests (during which it got up to 220PSI). It now stops at 80PSI due to
(this was revealed during the autopsy) a damaged rubber seal which was due
to excessive heat. 9/30/02: Insulated the gun cables using electrical tape, squared off the gun mount sides and the injector rails at the mill, bolted the injector end plate in place, screwed the tank in (a process which involved taking the injector off the mount and gun) and did a few 100PSI test firings. The gun is now COMPLETE!!!
The finished Device:
Honestly, I think the gun looks better (cleaner, lighter) without that huge air tank next to it, but since this is about functionality more than looks, it'll stay. I am currently investigating the possibility of running a full unregulated Nitrogen gas tank line (that's almost 3000PSI) to the injector through a special valve for supersonic injection velocities, but for now this is what the gun will look like. Tomorrow I hope to finally test fire it at high pressures and video it. 9/28/02: Machine shop is closed today but with no time to waste I shrink wrapped the gun wires in my dorm room. 9/28/02: Bought coaxial connectors and heat shrink tubing at Radio Shack. I will use coax connectors to connect the charger to the capacitor bank, and insulate the rail gun connections with heat shrink. $14. 9/27/02: 7 hours of machine shop work today. First I shortened the two 1/2" polycarbonate sheets that rise the gun from its mount so as to make the gun lower; this will provide less angular momentum at the base and the reduced torque will make it less likely for the gun to break off its mount due to recoil. I than cut 2 square 1/4" thick polycarbonate sheets, glued them to the gun mount risers, glued the risers to the base, drilled 4 holes in each sheet, so now the gun bolts to the mount through them. I noticed one of the rails was slightly behind the muzzle of the gun, so I had to loosen every single bolt, realign them, and than re-tighten all the bolts. I removed the injector, drilled 4 holes in the back, an threaded them to 10 - 24. Also drilled and countersunk 4 holes on the injector back plate. Now all that is left to do is square off the sides of the mounting brackets on the mill, square off the back of the Teflon injector rails, screw the back plate on, screw the tank onto the back plate, insulate the wires coming out of the gun and hook it up to the capacitor bank (not yet completed). This weekend I will insulate the gun wires, and MONDAY it will be COMPLETE and READY TO FIRE! I will try and hydrostatically test the tank to 300PSI and celebrate by testing the injector/gun assembly with compressed air at that pressure (If the compressor collaborates). Everything is looking SOOO good, but I won't post any pictures until the gun is ready now; this page is getting too large.
9/26/02: 5 hours of machine shop work again today; First I melted the old solder out of the damaged rail, sandblasted it clean, flushed it and re-soldered 8 new wires on. Than I milled both rails smooth again (excess solder and heat made their surfaces somewhat irregular) and fitted them on the gun. Using a router I cut all the screw heads on the injector flush, measured and cut a 1/2" polycarbonate sheet for form a 1 foot long, 1" high base for it. This base will attach the gun to its power supply. I still need to glue the base together and mill the plates it will use to bolt on to the gun, than I will fit the end plate onto the injector, polish the rails, insulate their first 2" with PFA film, bolt everything together and it will be ready to go! I should have everything ready by Friday. Next week the complete Rail Gun will be test fired using compressed air at the system's maximum capacity. A good day at last :)
9/25/02:
I thought yesterday was a bad day but hey, what do you know; in light
of today yesterday doesn't even look that bad any more; start off with
trying to solder eight AWG 8 oxygen free high current wires on a .200"
slot in an oxygen free copper rail using an oxygen/acetylene torch; first
the wires wouldn't go in the slot, than the solder wouldn't melt (high
silver content 1100F solder), finally a lower temperature solder did melt
but wouldn't adhere. The end result? 16 feet of expensive wire wasted and
a rail potentially ruined.
If I can't sandblast it clean tomorrow I will have to build a whole new
rail. The second rail soldered fine though. Then comes cutting seven 1'
long, 2.5" wide 0.064" thick oxygen free copper buss bars for the
capacitor bank using a guillotine-type sheet metal cutter; first of all it
was very difficult given that the material was thicker than what the
cutter was designed for. Secondly, a measurement mistake means now I only
have 6 bars, and will have to order a new sheet of copper just to cut a
single bar from it.
9/24/02: Some days it is just not my day... Tried drilling 8 holes in each rail to make the connections for the 8AWG oxygen free wires and ended up breaking 2 drill bits. The second one actually EXPLODED and sent drill shrapnel all over the machine shop. All that at a measly 1600RPM (I don't think that's unreasonable at all for copper, even without coolant, and the shavings I was getting didn't seem to be discolored). Ended up spending 3 hours to remove the drill bits and mill slots on the rails as opposed to having 8 separate holes. The rails are all irregular in the ends now. I'll solder the wires on them with high temperature silver solder and than have to mill them again. Hopefully this will all happen tomorrow... If I can make a mount for the gun too that'd make my day, but I probably won't have the time :-/
9/23/02:
Again 5 hours of machine shop work today (3:30PM - 8:30PM, no dinner). I
started off by recovering the 1300cc air tank from the paint booth,
re-attaching the solenoid to the valve and the reducer to the valve exit
(they were removed so as not to be painted) and wiring the solenoid for AC
duty. I than borrowed a variable 0 - 20V 0-30A DC power supply to run the
air pump and hooked it up to the valve on the tank. The first attempt at
pumping it up resulted in the rubber hose disconnecting from the pump at
220PSI and flapping all over the place. I fixed it by holding it
with a brace for the next run. The second attempt resulted in the hose
breaking off the pump at 80PSI. Again I braced it, but this time I was
more careful to place the brace further back on the connection. For the
3rd run the pump functioned for a few minutes, reached 195PSI, and than
went up in smoke! I guess I couldn't expect *too* much from a 13 dollar
pump... Either way, with 195PSI in the tank I placed a 8" ^2 1" thick
wooden block one and a half feet away from the reducer and opened the
valve to get a feel for the flow it lets through at that pressure. The
results were very satisfactory! The blast of highly compressed air was
powerful enough to send the block flying across the machine shop! I look
forward to testing the entire assembly (injector in place on the RailGun)
perhaps by the end of the week when I receive new spacers. For now this is
all the work I am doing with the tank. Click here to watch an .mpg (1.2MB)
video of the test at 195PSI.
9/21/02: Today I purchased 30 feet of AWG 8 Oxygen Free high current cable. I will use 8 pieces of this cable in parallel per rail to connect the gun to the capacitor bank. Ideally I should be using AWG 6 but this will do.
9/20/02: Went out today and bought a 12V 250PSI pump, as well as a 1/4" nipple for connecting the compressor to the air tank. The connector was first smeared in epoxy, than threaded into the cap, which received a second coating of epoxy, than a steel washer, another coating of epoxy, and finally a steel nut. This should ensure that the thread at the nipple is not a point where failure can occur in the tank. Once the tank was completed I cleaned it with PVC pipe cleaner and gave it a through coat of glossy black spray paint at the mechanical engineering building paint booth. You'll have to wait until Monday to see what the finished product looks like, and hopefully than I will perform hydrostatic testing on it and if all goes well, test fire the injector.
9/19/02: Worked at the machine shop today
for 5 hours and produced an air tank for my injector.
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2 FT |
8735K262 |
Teflon Rectangular Bar 1/4" Thick, 1-1/2" Wide, 2' Length |
$14.07 |
$28.14 |
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1 EA |
4738K157 |
Brass Solenoid Valve 1/2" NPT Female, 115 VAC |
$54.19 |
$54.19 |
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1 EA |
89675K43 |
Alloy 101 Oxygen-Free Copper Sheet .064" Thick, 12" X 24" |
$71.49 |
$71.49 |
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1 EA |
8574K32 |
Polycarbonate Sheet 1/2" Thick, 12" X 12", Clear |
$17.05 |
$17.05 |
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Merchandise Total: |
$170.87 |
So far I still need to get clearance to use the Lathes, the CNC mill (that takes a long time, given the complexity of the machine), and the welding machines (MIG and Oxy-Acetylene). If I decide to machine the G-9 rail holder I will probably do it here since it will require carbide cutters and drills.
My advisor, Dr. Brad King, made available for me this table on the laboratory, along with storage space for the material I obtained so far. The table sits next to a massive high vacuum chamber where Ion propulsion engines and other forms of advanced space propulsion are tested.
Some of the power supplies available in the laboratory include low and high voltage DC and AC stabilized and current/voltage monitored power rack supplies used to feed the Ion Engines and the vacuum chamber line degassing heaters. I will most probably be building my own capacitor charging supply for the gun however, since I want it to be portable and self contained.
The vacuum chamber by far occupies the most space in the laboratory. It is connected to a very large 2-stage water cooled oil sealed rotary pump which than connects to a very large Liquid Helium cryopump. The entire system is designed to run for days at a time testing ionic and plasma propulsion engines. Although I won't be using it for my project (though I haven't completely ruled out the possibility of hiding inside it when the gun is fired for the first time:) ) it will probably be featured in most of my lab pictures since it pretty much takes up the whole room. I would love to test some of my own plasma propulsion ideas on that chamber some later time, but for now my complete focus is on the RailGun project.
1 EA |
88865K312 |
Alloy 110 Silver-Plated Copper Rectangle 1/4" Thick, 1-3/8" Width, 3' Length |
$19.10 |
$19.10 |
today |
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1 EA |
8574K85 |
Polycarbonate Sheet 1/4" Thick, 48" X 48", Clear |
$90.35 |
$90.35 |
today |
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1 FT |
84955K12 |
PFA Film .001" Thick X 24" Wide |
$3.93 |
$3.93 |
today |
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4 FT |
8735K25 |
Teflon Rectangular Bar 1/4" Thick, 1" Wide |
$9.41 |
$37.64 |
today |
||
1 EA |
8661K127 |
Grade G-9 Garolite Sheet 1/2" Thick, 12" X 12", Gray-Brown |
$54.81 |
$54.81 |
today |
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1 PK |
91286A196 |
Ultra-Coated Grade 8 Hex Head Cap Screw 5/16"-24 Thread, 2-1/2" Lg |
$5.96 |
$5.96 |
today |
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25 EA |
93915A140 |
High-Pressure Self-Sealing Locknut 5/16"-24 Screw Sz, Fine Thread, 9/16" WD, 17/64" HT |
$3.40 |
$85.00 |
today |
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1 PK |
98180A120 |
Ultra Coated High Strength Steel Washer 5/16" Screw Size, 11/32" ID, 11/16" OD,.051" Min Thick |
$2.60 |
$2.60 |
today |
||
10 EA |
91740A104 |
Thread Restoring Bolt 1/4"-20 Coarse Thread X 1-1/4" Long |
$3.47 |
$34.70 |
today |
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Merchandise Total: |
$334.09 |
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I ended up paying $394 with the shipping. These will allow me to make the capacitor box (48x48" polycarbonate sheet) and the rail enclosure (G-9 Garolite, Teflon spacer, PFA insulator, bolts, nuts, washers, etc), The rails will be made from the copper rectangle. I still need parts for the power supply; V and A meters, bleeder resistors, discharge switches, high voltage cables, inverter, etc... Anyone have any of this stuff?
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Testing: |
All videos are .MPG format. For
powered testing videos go to the Rail Gun
Testing Page.
195PSI air
tank/valve/reducer test video (1.2mB; a blast of air blows a
wooden block across the room). |
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Comments? Mail me. People have visited this page since 30/01/00. Last updated 11/02/10 |
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� 2002 by Sam Barros. All rights reserved. Removing any material from this site for display without consent from its author consists in an infringement of international copyright laws and can result in fines up to $50000 per infringement, plus legal costs. So ASK ME before you remove anything from here. |